Celeros Flow Technology has injected new life right into a heritage pump for a Canadian heavy oil restoration buyer, enabling them to increase manufacturing. The pump – a Mather & Platt BB5 – was more than forty years outdated and had been subject to quite a few post-installation alterations.
เกจวัดแรงดันน้ําไทวัสดุ are extremely viscous and require the injection of high pressure, high temperature steam to improve fluidity and allow the oil to be pumped to the surface. In order to boost extraction on this venture, the shopper wanted to extend water temperatures from 90° C to 140° C. However, there have been issues that the present pump might not have the ability to ship this requirement. Nozzle masses have been a selected concern. They turned to Celeros Flow Technology model ClydeUnion Pumps, their most popular provider of some 20 years, for help.
Mather & Platt is certainly one of several heritage pump manufacturers for which Celeros Flow Technology presents full lifecycle support1. Their aftermarket engineering team undertook a thorough examination of the quadragenarian Steam Assisted Gravity Drainage (SAGD) boiler feed water pump used in the heavy oil extraction process. The investigation revealed that the pump had suffered a number of seal failures over time that had damaged the stuffing box and affected operational efficiency. There had additionally been no upkeep interventions for decades – but the pump had never really failed.
Says Mike Golds, Global Upgrade and Rerate Programme Manager for ClydeUnion Pumps: “It is testament to the standard of the unique pump that it had continued to function in such harsh conditions and with no common maintenance over such an extended time period. More importantly, it gave us confidence that a thorough overhaul may obtain the desired enchancment in performance, saving the client the price and lost production time that can be related to sourcing and putting in a new unit.”

Celeros Flow Technology overhauled the SAGD pump and performed a mechanical seal improve and Plan 23 seal flush to optimize pump efficiency. In addition, finite factor evaluation was undertaken to confirm that the nozzle loads would face up to the desired temperature increase. As a outcome, the pump is now capable of delivering steam at the higher temperatures required. The seal upgrades ensure it meets the most recent specifications.
Concludes Mike Golds: “We are really happy with the finish result of the SAGD pump upgrade. It has not solely achieved the specified production improve for the shopper, but also offered a extra sustainable and cost-effective answer than complete pump substitute. Using modern engineering and analysis, we now have been able to give the prevailing pump a model new lease of life and guarantee it’ll proceed to carry out properly for many more years.”

Share

Leave a Reply